The VTI National Transport Library Catalogue

Long-span guardrail system for culvert applications Faller, Ronald K et al

By: Faller, Ronald KPublication details: Transportation Research Record, 2000Description: nr 1720, s. 19-29Subject(s): USA | Safety fence | Culvert | | Performance | | 34Bibl.nr: VTI P8167:1720Location: Abstract: A long-span guardrail for use over low-fill culverts was developed and successfully crash tested. The guardrail system was configured with 30.48 m of nested, 12-gauge W-beam rail and centered around a 7.62-m-long unsupported span. The nested W-beam rail was supported by 16 W152 x 13.4 steel posts and 6 standard CRT posts, each with two 150-mm x 200 x 360 mm wood block-outs. Each post was 1830 mm long. Post spacings were 1905 mm on center, except for the 7.62-m spacing between the two CRT posts surrounding the long span. The research study included computer simulation modeling with Barrier VII and full-scale vehicle crash testing, using 3/4-ton (680-kg) pickup trucks in accordance with the Test Level 3 (TL-3) requirements specified in NCHRP Report 350. Three full-scale vehicle crash tests were performed. The first test was unsuccessful because of severe vehicle penetration into the guardrail system. This penetration resulted from a loss of rail tensile capacity during vehicle redirection when the swagged fitting on the cable anchor assembly failed. A second test was performed on the same design, which contained a new cable anchor assembly. During vehicle redirection, the pickup truck rolled over and the test was considered a failure. The long-span system was subsequently redesigned to incorporate double block-outs on the CRT posts and crash tested again. Following the successful third test, the long-span guardrail system was determined to meet TL-3 criteria.
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A long-span guardrail for use over low-fill culverts was developed and successfully crash tested. The guardrail system was configured with 30.48 m of nested, 12-gauge W-beam rail and centered around a 7.62-m-long unsupported span. The nested W-beam rail was supported by 16 W152 x 13.4 steel posts and 6 standard CRT posts, each with two 150-mm x 200 x 360 mm wood block-outs. Each post was 1830 mm long. Post spacings were 1905 mm on center, except for the 7.62-m spacing between the two CRT posts surrounding the long span. The research study included computer simulation modeling with Barrier VII and full-scale vehicle crash testing, using 3/4-ton (680-kg) pickup trucks in accordance with the Test Level 3 (TL-3) requirements specified in NCHRP Report 350. Three full-scale vehicle crash tests were performed. The first test was unsuccessful because of severe vehicle penetration into the guardrail system. This penetration resulted from a loss of rail tensile capacity during vehicle redirection when the swagged fitting on the cable anchor assembly failed. A second test was performed on the same design, which contained a new cable anchor assembly. During vehicle redirection, the pickup truck rolled over and the test was considered a failure. The long-span system was subsequently redesigned to incorporate double block-outs on the CRT posts and crash tested again. Following the successful third test, the long-span guardrail system was determined to meet TL-3 criteria.

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